Scaled Composites Pond Racer
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The Scaled Composites Pond Racer was an aircraft developed for Bob Pond by Burt Rutan and his company Scaled Composites. Designated Model 158 it was a twin-engine twin-boom design similar in some ways to the Lockheed P-38 attack fighter of World War II.
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[edit] Reason for creation
Bob Pond commissioned the design with the idea of developing a modern aircraft that could compete with the vintage warbirds in the Unlimited Class at the Reno air races. Bob Pond was concerned that each year at the Reno Air Races, valuable and historic aircraft were being crashed and destroyed, not to mention many engines being damaged or wrecked beyond repair. The Pond Racer was hoped to be an alternative to vintage aircraft like the P-51 Mustang and the Hawker Sea Fury that would be as fast and spectacular in the air as the warbirds.
[edit] Design
The airframe was constructed of composite materials, carbon fiber and Kevlar. This resulted in a very light, strong aircraft. To power the plane two Electramotive 3 liter V-6 engines were chosen. These were based on the Nissan VG30 automobile engine. The engines were originally developed for auto racing and were turbocharged to produce 1,000 hp (750 kW). However, those fitted to the Pond Racer only ever achieved a peak of around 600 hp (450 kW). The engines drove 4 bladed propellers via propeller speed reduction units (PSRU).
[edit] Aircraft Debut
The aircraft made its debut at the 1991 Reno air races having been flown from the Scaled Composites factory under escort. The plane was ferried burning gasoline for maximum distance potential and the onboard engine control computers were swapped out for metering methanol for race configuration. Methanol was the preferred fuel because no intercoolers were needed, and so the associated drag was obviated. After the day's running had concluded the engines were again configured to burn gasoline to preclude the corrosive effects of methanol. The aircraft was entered in the Silver class and qualified at 400 mph (640 km/h), flown by experienced test pilot Rick Brickert. The aircraft developed mechanical problems before the race was officially started and dropped out as a DNS.
The decision was made by Pond to attend Reno with the same engines used for flight testing. In fact, a vibrator was still attached to the left vertical stabilizer to initiate flutter as part of the planned flight test program. There was no expectation of victory the first year. It was viewed as a "dress rehearsal" more than anything else. After takeoff for the final event on Sunday, the left engine threw a rod out the side of the block and created a tunnel of fire 4 feet (1.2 m) in diameter and about 15 feet (4.6 m) long. An onboard halon extinguishing system put the oil fire out and an uneventful single-engine landing was made. The engine installations were very compact and "close cowled", meaning the bodywork covering the engines had little clearance. The carbon fiber engine cowling was a structural component of the aircraft and as such had to be protected from heat-soak after shutdown. This was accomplished via two 2-stroke weed blowers immediately after the blades stopped turning, quickly followed by two air conditioner blowers attached to the air inlet "scuppers". The engine cowlings were lined with corrugated inconel of .007 thickness. Airflow was vital to structural integrity. Conversely, the powerplant units had to be preheated to nearly operating temperature before fireup. This was due to the tight tolerances of the engine main bearings. Because methanol burns much cooler than gasoline, cooling was never an issue. Actually the cold nature of the methanol gave the team a problem with oil viscosity. The thick, graphite laden oil would "puke" overboard for the majority of the the time while airborne. Eventually it was determined that the oil drain holes were undersized in the rocker area of the heads as they were not intended to run at a constant high RPM in an automobile application. Fully half of the radiator inlet ducting was blocked off after the first test flight on March 22, 1991. Dick Rutan was the initial test pilot. Mike Melvill also flew the plane as did Steve Hinton as part of the test program.
[edit] Problems and tragedy
The Pond Racer was entered the following year and seemed to finally be showing some promise achieving second place in the bronze class in the hands of Rick Brickert. To help alleviate the cooling problems, large blowers were used on the ground when the plane was started up, to force air through the cooling system until the aircraft could be taxied out and flown.
In 1993 the Pond racer was entered again and once more, piloted by Rick Brickert. During qualifying, the aircraft began leaking oil and suffered an engine failure. The margin for error in pylon racing is very small as the competitors fly close to the ground at high speed. The Pond Racer crashed and killed Rick Brickert.
Rick was a very popular figure and a personal friend of Bob Pond. The Pond racer project was never revived and a modern unlimited class challenger was never truly realized.