Quad Cities Nuclear Generating Station

From Wikipedia, the free encyclopedia

NRC
Region Three
(Midwest)
Illinois
Braidwood
Byron
Clinton
Dresden
LaSalle County
Quad Cities
Iowa
Duane Arnold
Michigan
Donald C. Cook
Enrico Fermi
Palisades
Minnesota
Monticello
Prairie Island
Ohio
Davis-Besse
Perry
Wisconsin
Kewaunee
Point Beach

This box: view  talk  edit

Quad Cities is a two-unit nuclear power plant located near Cordova, Illinois, USA on the Mississippi River. The two General Electric boiling water reactors give the plant a total electric capacity of approximately 1,824 MW. It was named for the nearby cities of Moline, East Moline, Rock Island, and—on the Iowa side of the Mississippi—Davenport,[1] which at the time of its construction in the early 1970s were known as the Quad Cities. (Neighboring Bettendorf, Iowa, has since been added to the ranks of the Quad Cities.) The Quad Cities plant is owned and operated by Exelon Corporation.

Unit 1     Nuclear system supplied by General Electric Company (U.S.)

Capacity
Net MW(e)
Generation
in 2003
Megawatt-hours
Capacity
Factor
Type
On-line
Date

License

Expiration Date
912
5,709,520
90.6 %
BWR
Dec. 14, 1972
Dec. 14, 2032
Unit 2      Nuclear system supplied by General Electric Company (U.S.)
Capacity
Net MW(e)
Generation
in 2003
Megawatt-hours
Capacity
Factor
Type
On-line
Date

License

Expiration Date
912
6,956,073
92.7  %
BWR
Dec. 14, 1972
Dec. 14, 2032

BWR= Boiling Water Reactor

[edit] Extended Power Uprate

During an extended power uprate test on March 5, 2002 designed to extend the power efficiency of existing BWR reactors the Quad Cities Nuclear Generating Station unit 2 (Illinois) began to experience vibrations in a steam line. On March 29 the plant was manually shut down due to high vibrations causing leaks in the main turbine control system. Unit 2 had a restart on April 2, but vibration broke a main steam pipe drain line. The line was repaired and the restart resumed but by June 7 the main steam lines were showing unexplained aberrations. On June 18 it became obvious that the power uprate was causing damage so the power was reduced but the damage had been done. Once again the plant was taken offline for repairs on July 11. The problem was traced to a hole in the steam dryer—it was repaired and braced, then unit 2 was restarted on July 21, 2002. The steam dryer failed again on May 28, 2003 with a ¾ in x 9 ft (20 mm by 2.7 m) crack. The incident did not result in any increased probability of an accident. The NRC inspected all repairs and the extended power uprate was completed successfully.[1]

[edit] References

  1. ^ NRC: SECY-01-0124 - Power Uprate Application Reviews

[edit] External links

Languages