Braniff Flight 352

From Wikipedia, the free encyclopedia

Braniff Flight 352
Summary
Date  May 3, 1968
Type  Pilot error, thunderstorm
Site  Dawson, Texas
Fatalities  85
Injuries  0
Aircraft
 Aircraft type  Lockheed L-188A Electra
Operator  Braniff
Tail number  N9707C
Passengers  80
Crew  5
Survivors  0

Braniff International Airways Flight 352 was a Lockheed L-188A Electra, registration N9707C, operating as a scheduled domestic flight from Houston to Dallas, Texas, that broke up in mid air and crashed near Dawson, Texas after flying into a severe thunderstorm on May 3, 1968. The 5 crew and 80 passengers on board were killed. Investigation revealed that the accident was caused by the captain's decision to penetrate an area of heavy weather followed by a structural overstress and failure of the airframe during a steep 180 degree diving turn executed in an attempt to escape the weather.[1]

Contents

[edit] Flight history

Earlier in the day, at 12:40 local time, the crew of the accident flight flew from Dallas to Houston through the same area they were scheduled to fly later on. On that previous flight, a few hours before, they encountered no significant weather along the route. Once they arrived in Houston, there was no record of the crew being briefed about the updated weather by any Weather Bureau or FAA personnel, or by any Braniff dispatcher or weather office. They did, however, receive hardcopy information about all relevant enroute and terminal weather reports and forecasts.

At 16:11, the crew departed Houston-Intercontinental Airport as Brannif Flight 352, a Lockheed L-188A Electra four-engine turboprop, enroute to Dallas-Love Field. After about 25 minutes into the flight, while cruising at FL200 (about 20,000 feet above mean sea level), the aircraft approached an area of severe thunderstorm activity. The crew requested to descend to FL150 and deviate to the west. ATC informed the crew that other flights in the area were deviating to the east and suggested they also deviate east, but the Electra crew insisted[2] that the west seemed OK to them on their onboard weather radar:

"Three fifty two does it look good (better). On our scope here it looks like to the uh a little just a little bit to the west would do us real fine."

ATC then cleared the flight to descend to FL140 and deviate to the west as they requested. (The westerly deviation would have been shorter and quicker than an easterly one.[3])

At 16:44 the crew requested and ATC cleared the flight to descend to 5,000 feet. The crew asked ATC if there were any reports of hail in the area, to which ATC replied:

"No, you're the closest one that's ever come to it yet . . . I haven't been able to, anybody to, well I haven't tried really to get anybody to go through it, they've all deviated around to the east."

At 16:47 the flight encountered an area of severe weather including hail and requested a 180 degree right turn, which ATC immediately approved. While turning to the right in severe turbulence the bank angle was increased to over 90 degrees, and the nose pitched down to approximately 40 degrees. As the crew attempted to recover from the ensuing steep diving turn, the aircraft experienced acceleration forces of over 4 g, which caused the right wing to fail. The aircraft then broke up at an altitude of 6,750 feet and crashed in flames into the ground at about 16:48, killing all 85 persons on board.[1][4]

[edit] Investigation

The NTSB investigated the accident. The flight data recorder (FDR) and cockpit voice recorder (CVR) were recovered from the wreckage with their data mostly intact, and the cockpit audio was reconstructed and transcribed.

The NTSB correlated the cockpit conversations with the ATC communications transcript and noted that it was the first officer, at the captain's request, who asked ATC about hail in the area and received the response from ATC that "no ... they've all deviated around to the east." At that point, according to the CVR transcript, the captain advised the first officer,

"No, don't talk to him too much. I'm hearing his conversation on this. He's trying to get us to admit (we're makin)[5] big mistake coming through here."

Shortly thereafter, the first officer stated: ". . . it looks worse to me over there." The crew then requested and received clearance from ATC for the 180 degree turn. The turn became extremely steep, with a bank of over 90 degrees and a nose pitch down of 40 degrees. As they were trying to recover from the turn, the FDR indicated a peak acceleration of 4.3 g, which the NTSB concluded caused a structural overstress and inflight breakup.
On June 19, 1969 the NTSB issued its final report, which included the following Probable Cause statement:[4]

"Probable Cause: The stressing of the aircraft structure beyond its ultimate strength during an attempted recovery from an unusual attitude induced by turbulence associated with a thunderstorm. The operation in the turbulence resulted from a decision to penetrate an area of known severe weather."

[edit] See also

[edit] References

  1. ^ a b Aviation Safety Network accident record. Retrieved on 2006-10-14.
  2. ^ Finding #15 in the NTSB report
  3. ^ Finding #26 in the NTSB report
  4. ^ a b NTSB Report.
  5. ^ Other possible interpretations for the parenthesized words which were garbled in the audio: "we'd made the" or "we made a"

[edit] External links

  • 1968.html - web site with photos and data relating to Braniff Flight 352, claiming accident was actually caused by inflight explosion covered up by factions at Braniff, and possible politicians with INFLUENCE at NTSB
  • Airliners.net Photo of Electra N9707C, in Dallas Love Field, in September 1962
  • Airliners.net Another photo of Electra N9707C, also in Dallas Love Field in February 1964