Bar Harbor Airlines Flight 1808
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Summary | |
---|---|
Date | August 25, 1985 |
Type | Controlled flight into terrain |
Site | Auburn, Maine |
Fatalities | 8 |
Injuries | 0 |
Aircraft | |
Aircraft type | Beech BE-99 |
Operator | Bar Harbor Airlines |
Tail number | N300WP |
Passengers | 6 |
Crew | 2 |
Survivors | 0 |
Bar Harbor Airlines Flight 1808 was a scheduled flight from Boston Logan International to Bangor International on August 25, 1985. The flight normally stopped enroute at Augusta and Waterville, Maine. The flightcrew flew the accident aircraft from Bangor to Boston and back earlier that afternoon in worsening weather. On the second trip they were advised at an enroute stop in Augusta that because of ATC delays in Boston their return flight 1788 via Auburn/Lewiston, Maine was being cancelled. They would instead operate the later flight 1808 with Auburn added as a flag stop to accommodate passengers from flight 1788.
Flight 1808 boarded in Boston with 6 passengers; 2 for Auburn, 3 for Augusta and 1 for Waterville. At 9:17 pm EDT the Captain radioed for their clearance to Auburn. The controller unaware of the change in routing advised they were filed to Augusta. The captain accepted the routing, but advised they would amend their routing after passing Pease VOR, near Portsmouth, New Hampshire to Auburn. They departed the ramp at 9:26 pm and were cleared for takeoff from runway 4L at 9:30 pm.
At 10:00 pm they radioed the station agent at Auburn/Lewiston Municipal Airport for the latest weather. The agent advised them the ceiling was 300' overcast, visibility 1 mile, wind 020 (North Northeast) at 4 knots, altimeter 30.24 InHg. Shortly after this the crew was advised by a controller in Portland they were drifting east of the ILS approach course to runway 4 at Auburn. He advised them to turn to heading 340 to intercept. The Captain responded "OK". Almost a minute later the controller advised them they were passing the Lewie NDB beacon at the outer marker for the approach and asked if they were receiving it. The first officer responded "affirmative". This was the last transmission received from the flight. Portland controllers were notified less then 10 minutes later the plane had crashed at 10:05 pm.
In the aftermath of the accident investigators were hindered by the absence of cockpit voice recorder and flight data recorder information. The Beech 99 was not a large enough plane for the FAA to require their installation. There was also no record of which pilot was to have flown the aircraft. Both pilots had used the radio during the flight instead of the non flying pilot. Examination of radar data from Portland showed that after the plane turned to course 340 to intercept the approach it flew through the approach and had to correct to get back on course. Investigators noted this instruction meant the flight crew had to make a 60 degree turn less then one mile from the approach outer marker. Altitude data transmitted by the aircraft transponder showed the plane did not begin its descent along the precision glide slope until it was above it after passing Lewie. This may have caused the flight crew to rush both the descent and the approach. The Captain's altimeter recovered from the wreckage was set to 30.42 InHg, a number transposition from the correct setting 30.24 InHg. With this setting it would have read approximately 180' higher then the plane actually was and close to the 200' above ground level minimum descent for the approach. The first officer's altimeter was also set incorrectly at 30.12 InHg causing it to read 120' low. The aircraft flew into trees less then one mile from the end of runway 4 and impacted the ground less then 500' to the right of the extended runway center line. There were no survivors.
In publishing its report the NTSB noted that the controller in Portland used "poor judgement" assisting the flight. However it concluded the Captain accepted the large course correction and the crew continued flying an unstabilized approach instead of executing a missed approach. Also the flight crew attempted to stabilize the approach while allowing the plane to fly below the instrument glide slope. The incorrect altimeter settings may have caused this descent to continue below the published decision height. At night in low visibility the crew may have been unaware of their true position. The NTSB recommended a review of controller procedures for outlying airports without ground radar. The 60 degree turn less then one mile from the outer marker would violate approach guidelines for radar assisted arrivals to Portland International Jetport for example. It further recommended aircraft for hire capable of carrying 6 or more passengers be equipped with flight recorders.
[edit] Notes
This accident attracted unusual media attention for a small commuter plane accident. The two passengers who had boarded in Boston for Auburn/Lewiston were Samantha Smith and her father Arthur Smith. A few years earlier Samantha had written Soviet Premiere Yuri Andropov of her desire for peace between the United States and the Soviet Union. At Andropov's invitation she and her family toured the Soviet Union and helped ease tensions between the two countries. In 1985 ABC television hired her to be an actress on its new show Lime Street which would be filmed on location in London. The accident happened as she was returning home from London with her father.
[edit] References
- Aircraft Accident Report AAR-86-6 (PDF) National Transportation Safety Board