Chinook helicopter crash

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Mull of Kintyre Chinook crash
Summary
Date   2 June 1994
Type   CFIT(?)
Site   Mull of Kintyre, Scotland
Fatalities   29
Injuries   0
Aircraft
Aircraft type   Boeing Chinook
Operator   Royal Air Force
Tail number   ZD576
Passengers   25
Crew   4
Survivors   0

On 2 June 1994 at about 1800hrs a Royal Air Force (RAF) Chinook helicopter ZD576 (callsign F4J40), carrying almost all the United Kingdom's (UK) senior Northern Ireland intelligence experts, crashed on the Mull of Kintyre, Scotland, killing all on board: 25 passengers and 4 crew members.

Contents

[edit] Case history

The twin-engined Chinook ZD576 flew into a hillside in dense fog. The area has been the site of many air crashes throughout its history.

Wreckage of ZD576
Enlarge
Wreckage of ZD576

'The initial point of impact was 810 feet above mean sea level and about 500 metres east of the lighthouse, but the bulk of the aircraft remained airborne for a further 187 metres horizontally north and 90 feet vertically before coming to rest in pieces. Fire broke out immediately. All those on board sustained injuries from which they must have died almost instantaneously. The points of impact were shrouded in local cloud with visibility reduced to a few metres, which prevented those witnesses who had heard the aircraft from seeing it.'[1]

The helicopter was carrying 25 British intelligence experts from MI5, the Royal Ulster Constabulary and the British Army, from RAF Aldergrove (outside Belfast, Northern Ireland) to attend a conference in Inverness in Scotland.

The official inquiry concluded that the crash was caused by pilot error, although this has often been disputed.

The incident has been the subject of controversy, partly because there was a dispute as to whether the crash was caused by pilot error or by mechanical failure following refit. The fact that the crash killed so many intelligence experts, and the fact that none of the witnesses actually saw the crash in the foggy conditions, encourage speculation over official cover-ups and conspiracy theories. An immediate suspicion that the helicopter could have been shot down by the Provisional Irish Republican Army with their known SA 7 surface-to-air missile capability was quickly ruled out by investigators.

Alternative theories point to problems with the RAF's upgrade program for their Chinook helicopters. In particular, other similarly upgraded helicopters had experienced problems with engine power delivery delays and false warnings, which may have been caused by control software. Such an event could have been a major distraction to the flight crew.

In 1995, an RAF board of inquiry found that there was no conclusive evidence to determine the cause of the crash. However, two air marshals, on reviewing the evidence, found the two pilots guilty of gross negligence.

This ruling proved highly controversial. A subsequent Fatal Accident Inquiry (1996), House of Commons Defence Committee report (2000) and Commons Public Accounts Committee have all either left open the question of blame or challenged the original conclusion. The campaign for a new inquiry was supported by the families of the deceased pilots (who were Flight Lieutenants Jonathan Tapper, 28, and Rick Cook, 30; both Special Forces pilots) and senior politicians, including former Prime Minister John Major and former Defence Secretary Malcolm Rifkind.

The new inquiry took place in the House of Lords from September to November 2001. The findings were published on January 31, 2002, and found that the verdicts of gross negligence on the two pilots were unjustified.[2]

[edit] ZD576 service history

Construction number B-868, RAF serial number ZD576 was originally delivered to the Royal Air Force as a Chinook HC.1 on 22 December 1984. It was returned to Boeing for upgrade and was re-delivered as a Chinook HC.2 on 21 April 1994. On arrival at RAF Odiham, its No.1 engine had to be replaced. On 10 May 1994, a post-flight fault inspection revealed a dislocated mounting bracket causing the collective lever to have restricted and restrictive movement. This resulted in a Serious Fault Signal being sent as a warning to other UK Chinook operating units. On 17 May 1994 emergency power warning lights flashed multiple times and the No.1 engine was again replaced. On 25 May 1994 a serious incident occurred indicating the No.2 engine was about to fail.[citation needed]

On 1 June 1994, the MoD test pilots at Boscombe Down refused to fly the Chinook HC.2 until engines, engine control systems and FADEC software were rectified on the model in RAF service.[citation needed] On Thursday 2 June 1994 it crashed.

[edit] Possible factors

[edit] Pilot error

Andrew Brookes, observes in his book Flights to Disaster (1996, ISBN 0-7110-2475-8) that although the true cause will never now be known, pilot error induced by fatigue is likely to have played a great part; the crew had been on flight duty for almost six hours before they started the crash flight, longer than would be acceptable on civilian transport helicopters.

Although much was made of the potential for engine control problems being caused by the recent upgrade, it is hard to see how that on its own could have made two experienced flight crew fly a helicopter full of VIPs into a known cliff face at over 150 mph. As Hansard put it in 2000:

'There is no evidence of any significant change of course and none of the decision, if any, that the crew made. When the crew released the computer from its fix on the Mull, the pilots knew how close to the Mull they were and, given the deteriorating weather and the strict visibility requirements under visual flight rules they should by that time already have chosen an alternative course. As they had not done so, they could, and, under the rules, should have either turned away from the Mull immediately or slowed down and climbed to a safe altitude'.[3]

The two engines were also found to have been at matched power settings during physical examination after the crash, making the FADEC scenario (see below) less likely.

The 'emergency power' setting had not been triggered, as would be expected if a control problem had been experienced.

Nine out of ten witnesses interviewed in the inquiry reported visibility being as low as 10-100m in fog at the time of the crash. The tenth witness, a yachtsman who was offshore, reported it as being 1 mile, though he is regarded as a less reliable witness as he changed his testimony. He was also, of course, at sea level. RAF Visual Flight Rules require the crew to have a minimum visibility of 1 km.

Steuart Campbell suggests in his book Chinook Crash (2004, ISBN 1-84415-074-7) that by failing to climb to safety altitude upon entering cloud, and making a navigational error in poor visibility, mistaking the fog signal station for the lighthouse, together caused the crash.

[edit] Upgrade problems

The FADEC engine control software was being upgraded on all RAF Chinook aircraft, as part of an upgrade from Chinook Mk 1 to Chinook Mk 2 capability. The Ministry of Defence successfully sued Textron, the manufacturers of the system, after a near-fatal Chinook crash caused by an uncommanded engine run-up in 1989.

EDS-SCICON was given the task of independently evaluating the software on the Chinook Mk2 FADECs in 1993, and according to the House of Commons report, "after examining only 18 per cent of the code they found 486 anomalies and stopped the review". The report also noted that "intermittent engine failure captions were being regularly experienced by aircrew of Chinook Mk 2s and there were instances of uncommanded run up and run down of the engines and undemanded flight control movements". However, this software was being used on operational aircraft.

Chinook tests at Boscombe Down by the MoD in 1994 reported the FADEC software to be "unverifiable and ... therefore unsuitable for its purpose" [4]

[edit] Navigation software

The onboard Tactical Air Navigation System was shown to have a considerable error in height at the time of the crash, which may have been caused by the pressure of the exploding aircraft.

[edit] Flight data recorder

No flight data recorder or cockpit voice recorder was fitted. Evidence about speed and height were derived from the position of cockpit dials in the wreckage, and from the disposition of the wreckage itself.

By 2002, all of the RAF's Chinooks were fitted with these devices.[5]

[edit] Political and military impact

The loss of so many top level of Northern Ireland intelligence officers in one stroke was a huge blow to the John Major government, temporarily confounding the anti-IRA campaign.[6]. Why so many top assets were travelling together on a military transport when other, safer, modes of transport were available, is a question that has never been publicly answered.

[edit] References

  1. ^ Circumstances of the accident UK Parliament, 2002. Accessed 3 November 2006
  2. ^ Chinook ZD 576 - Report UK Parliament, 2002. Accessed 3 November 2006
  3. ^ MULL OF KINTYRE UK Parliament, 2002. Accessed 3 November 2006
  4. ^ PART 3: FACTUAL BACKGROUND UK Parliament, 2002. Accessed 3 November 2006
  5. ^ Helicopters UK Parliament, 2005. Accessed 3 November 2006
  6. ^ BBC News Accessed 3 November 2006

[edit] External links

[edit] Sources

  • McMullon, D (1998). Chinook! The Special Forces Flight in War and Peace. Simon & Schuster, 258pp + ix, ISBN 0-684-84017-0